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Rear Lifting Motor Circuit CheckAIS002XQ
1. CHECK REAR END SEAT LIFTING MECHANISM
Check the following.
Operation malfunction caused by lifter mechanism deformation or pinched harness or other foreign mate-
rials
Operation malfunction caused by foreign materials adhered to the lifter motor or lead screws
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “SEAT LIFTER RR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Rear lifting motor check is OK.
NG >> GO TO 3.
3. CHECK REAR LIFTING HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect driver seat control unit connector and rear lifting motor connector.
3. Check continuity between driver seat control unit connector B153 terminals 6, 7 and lifting motor connector B162 terminals
6, 7.
4. Check continuity between driver seat control unit B153 terminals 6, 7 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness between driver seat control unit and rear lifting motor.
Test item Description
SEAT LIFTER RR The rear end lifter motor is activated by receiving the drive sig-
nal.
PIIA0274E
6 (G/W) – 6 (G/W) : Continuity should exist.
7 (G/B) – 7 (G/B) : Continuity should exist.
6 (G/W) – Ground : Continuity should not exist.
7 (G/B) – Ground : Continuity should not exist.
PIIA6123E
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4. CHECK DRIVER SEAT CONTROL UNIT OUTPUT SIGNAL
1. Connect the driver seat control unit connector.
2. Rear lifting switch operate, check voltage between driver seat control unit connector and ground.
OK or NG
OK >> Replace rear lifting motor.
NG >> Replace driver seat control unit.
Telescopic Motor Circuit CheckAIS002Y9
1. CHECK STEERING WHEEL TELESCOPIC MECHANISM
Check following.
Operation malfunction caused by steering wheel telescopic mechanism deformation or pinched harness
or other foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part and check again.
2. CHECK FUNCTION
With CONSULT-II
Check operation with “TELESCO MOTOR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Steering telescopic motor circuit is OK.
NG >> GO TO 3.
Connector Te r m i n a l s
(Wire color) Rear lifting switch condition Voltage (V)
(Approx.)
(+) (–)
B153 6 (G/W)
Ground UP Battery voltage
Other than above 0
7 (G/B) DOWN Battery voltage
Other than above 0
PIIA6122E
Test item Description
TELESCO
MOTOR The telescopic motor is activated by receiving the drive signal.
PIIA0277E
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3. CHECK TELESCOPIC MOTOR HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit and tilt motor and telescopic motor connector.
3. Check continuity between automatic drive positioner control unit connector M50 terminals 36, 44 and tilt motor and telescopic
motor connector M27 terminals 3, 4.
4. Check continuity between automatic drive positioner control unit connector M50 terminals 36, 44 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness between automatic drive positioner control unit and tilt motor and tele-
scopic motor.
4. CHECK BCM OUTPUT SIGNAL
1. Connect the automatic drive positioner control unit connector.
2. Telescopic switch operate, check voltage between automatic drive positioner control unit connector and ground.
OK or NG
OK >> Replace tilt and telescopic motor.
NG >> Replace automatic drive positioner control unit.
Tilt Motor Circuit CheckAIS002YA
1. CHECK STEERING WHEEL TILT MECHANISM
Check following.
Operation malfunction caused by steering wheel tilt mechanism deformation or pinched harness and
other foreign materials
Operation malfunction and interference with other parts by poor installation
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning part. 36 (L/R) – 3 (L/R) : Continuity should exist.
44 (L/W) – 4 (L/W) : Continuity should exist.
36 (L/R) – Ground :Continuity should not exist.
44 (L/W) – Ground :Continuity should not exist.
PIIA5066E
Connector Terminals
(Wire color) Telescopic switch condition Voltage (V)
(Approx.)
(+) (–)
M50 36 (L/R)
Ground FORWARD Battery voltage
Other than above 0
44 (L/W) BACKWARD Battery voltage
Other than above 0
PIIA5068E
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2. CHECK FUNCTION
With CONSULT-II
Check operation with “TILT MOTOR” in ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Steering tilt motor circuit is OK.
NG >> GO TO 3.
3. CHECK TILT MOTOR CIRCUIT HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit connector and tilt and telescopic motor connector.
3. Check continuity between automatic drive positioner control unit connector M50 terminals 35, 42 and tilt and telescopic motor
connector M27 terminals 1, 2.
4. Check continuity between automatic drive positioner control unit connector M50 terminals 35, 42 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness between automatic drive positioner control unit and tilt and telescopic
motor.
Test item Description
TILT MOTOR The tilt motor is activated by receiving the drive signal.
PIIA0280E
35 (R/L) – 1 (R/L) : Continuity should exist.
42 (R/B) – 2 (R/B) : Continuity should exist.
35 (R/L) – Ground : Continuity should not exist.
42 (R/B) – Ground : Continuity should not exist.
PIIA5065E
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4. CHECK BCM OUTPUT SIGNAL
1. Connect automatic drive positioner control unit connector and tilt and telescopic motor connector.
2. Tilt switch operate, check voltage between automatic drive positioner control unit connector and ground.
OK or NG
OK >> Replace tilt and telescopic motor.
NG >> Replace automatic drive positioner control unit.
Driver Side Mirror Motor Circuit CheckAIS003BU
1. CHECK DOOR MIRROR FUNCTION
Check the following.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again.
2. CHECK MIRROR MOTOR
With CONSULT-II
Check the operation with “MIRROR MOTOR LH” in the ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Driver side mirror motor circuit is OK.
NG >> GO TO 3.
Connector Terminals
(Wire color) Tilt switch condition Voltage (V)
(Approx.)
(+) (–)
M50 35 (R/L)
Ground UP Battery voltage
Other than above 0
42 (R/B) DOWN Battery voltage
Other than above 0
PIIA5067E
Test item Description
MIRROR MOTOR LH The LH mirror motor moves the mirror UP/DOWN and
LEFT/RIGHT by receiving the drive signal.
PIIA4784E
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3. CHECK DOOR MIRROR MOTOR (DRIVER SIDE) HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit connector and door mirror (driver side) connector.
3. Check continuity between automatic drive positioner control unit connector M49 terminal 16, 31, 32 and door mirror (driver side)
connector D2 terminal 8, 9, 10.
4. Check continuity between automatic drive positioner control unit connector M49 terminal 16, 31, 32 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness between automatic drive positioner control unit and door mirror (driver side).
4. CHECK MIRROR MOTOR SIGNAL
1. Connect automatic drive positioner control unit and door mirror (driver side) connector.
2. Turn ignition switch ACC.
3. Turn change over switch LH position.
4. Mirror switch operate, check voltage between door mirror (driver side) connector and ground.
OK or NG
OK >> Replace door mirror motor (driver side).
NG >> Check the condition of the harness and the connector.
Passenger Side Mirror Motor Circuit CheckAIS003BV
1. CHECK DOOR MIRROR FUNCTION
Check the following.
Operation malfunction caused by a foreign object caught in door mirror face edge.
OK or NG
OK >> GO TO 2.
NG >> Repair the malfunctioning parts, and check the symptom again. 16 (P) – 8 (P) : Continuity should exist.
31 (R/W) – 10 (GY) : Continuity should exist.
32 (G/B) – 9 (PU) : Continuity should exist.
16 (P) – Ground : Continuity should not exist.
31 (R/W) – Ground : Continuity should not exist.
32 (G/B) – Ground : Continuity should not exist.
PIIA6131E
Connector Terminals
(Wire color) Mirror switch condition Voltage (V)
(Approx.)
(+) (–)
D2 8 (P)
Ground DOWN or RIGHT Battery voltage
Other than above 0
9 (PU) LEFT Battery voltage
Other than above 0
10 (GY) UP Battery voltage
Other than above 0
PIIA6130E
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2. MIRROR MOTOR INSPECTION
With CONSULT-II
Check the operation with “MIRROR MOTOR RH” in the ACTIVE TEST.
Without CONSULT-II
GO TO 3.
OK or NG
OK >> Passenger side mirror motor circuit is OK.
NG >> GO TO 3.
3. CHECK DOOR MIRROR MOTOR (PASSENGER SIDE) HARNESS CONTINUITY
1. Turn ignition switch OFF.
2. Disconnect automatic drive positioner control unit connector and door mirror (passenger side) connector.
3. Check continuity between automatic drive positioner control unit connector M49 terminal 14, 15, 30 and door mirror (passenger
side) connector D32 terminal 8, 9, 10.
4. Check continuity between automatic drive positioner control unit connector M49 terminal 14, 15, 30 and ground.
OK or NG
OK >> GO TO 4.
NG >> Repair or replace harness between automatic drive positioner control unit and door mirror (pas-
senger side).
Test item Description
MIRROR MOTOR RH The RH mirror motor moves the mirror UP/DOWN and
LEFT/RIGHT by receiving the drive signal.
PIIA0202E
14 (L/W) – 10 (PU) : Continuity should exist.
15 (L/B) – 9 (OR) : Continuity should exist.
30 (W/R) – 8 (GY) : Continuity should exist.
14 (L/W) – Ground : Continuity should not exist.
15 (L/B) – Ground : Continuity should not exist.
30 (W/R) – Ground : Continuity should not exist.
PIIA6133E
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4. CHECK MIRROR MOTOR SIGNAL
1. Connect automatic drive positioner control unit and door mirror (passenger side) connector.
2. Turn ignition switch ACC.
3. Turn change over switch RH position.
4. Mirror switch operate, check voltage between door mirror (passenger side) connector and ground.
OK or NG
OK >> Replace door mirror motor (passenger side).
NG >> Check the condition of the harness and connector.
Sliding Sensor Circuit CheckAIS002XS
1. CHECK FUNCTION
With CONSULT-II
Check operation with “SLIDE PULSE” on the DATA MONITOR to make sure the pulse changes.
Without CONSULT-II
1. Turn ignition switch OFF.
2. Check signal between driver seat control unit connector and ground, with oscilloscope.
OK or NG
OK >> Sliding sensor circuit is OK.
NG >> GO TO 2.
Connector Terminals (Wire color)
Mirror switch condition Voltage (V)
(Approx.)
(+) (–)
D32 8 (G/Y)
Ground DOWN or RIGHT Battery voltage
Other than above 0
9 (OR) LEFT Battery voltage
Other than above 0
10 (PU) UP Battery voltage
Other than above 0
PIIA6132E
Monitor item
[OPERATION or UNIT] Contents
SLIDE PULSE The seat sliding position (pulse) judged from the sliding sensor
signal is displayed.
PIIA4558E
Connector Te r m i n a l s
(Wire color) Condition Signal
(Reference value)
(+) (–)
B152 18 (G) Ground Sliding
motor
operation
PIIA6105EPIIA3277E